A loose lid on a rail utility box is suspected of causing a light-rail train to derail Thursday in downtown Minneapolis, forcing Metro Transit to halt service between Target Field Station and U.S. Bank Stadium for more than eight hours.
No one was injured in the derailment, the third in Metro Transit history for trains in service. As the evening rush hour came and went, downtown trains remained out of commission. Around 7 p.m., the derailed westbound Blue Line train was placed back on the tracks, and after a final inspection, trains began moving again about 7:35 p.m.
The three-train car jumped the tracks on S. 5th Street between 2nd and 3rd avenues S. shortly after 11 a.m. It buckled and came to rest under the skyway connecting the CenturyLink building and U.S. Bank Plaza. Through the day, the scene attracted hundreds of passersby who stopped to gawk and take photos.
No major damage to the train, the track or overhead power lines was reported, and replacement buses shuttled passengers to light-rail stations all day.
Preliminary indications are that the lead car passed over an insecure lid on a rail access box — a shoe-size utility box that houses electrical equipment — during routine maintenance and jostled it loose, then the wheels on the second car got stuck, said Metro Transit spokesman Drew Kerr.
Light-rail derailments have been unusual since the Blue Line began service in 2004 and the Green Line in 2014. In September 2014, a Blue Line car derailed between Terminal 2 of the Minneapolis-St. Paul International Airport and the Mall of America because of debris on the LRT tracks. No one was injured, and hundreds of commuters were transferred onto buses.
In March 2011, another Blue Line train derailed before midnight between the Nicollet Mall and Hennepin Avenue stations. At the time, Metro Transit said the mishap was weather-related.
'There was a jolt'
On Thursday, maintenance work was being done between passing trains by an unidentified contractor. Lids were to be placed back on the boxes, which are similar to manholes, but one was not properly secured, according to Metro Transit spokesman Howie Padilla. The work was part of maintenance that has been ongoing since last summer.